Nozzle Failure at
70,000’
by Jim Flemming,
Canberra
In 1958, being
the first TAC squadron to be re-equipped with the F104C Starfighter, the 476th
TFS had to do a lot of operational
testing of tactics, procedures and capabilities. These included Phase 2 nozzle
tests and high altitude operations.
There had been
a spate of nozzle failures in the J79 engine fitted to the F104C. It was found
that the nozzles, being operated by the engine oil system, were failing to open
or close due to sludge on the oil filters, The
system was changed so that the nozzles were controlled by the engine fuel
system and the problem was solved. The aircraft were being
modified at the next major inspection so some squadron aircraft continued
to operate with without the oil system control being modified..
For the high
altitude tests we were fitted with the early “Moonsuit” pressure suit which
was based on the same principle as the “G Suit”but with a full body fitting.
Prior to donning the pressure suit you were required to be powdered all
over with talcum powder and then don long underwear, inside out, so that the
seams would not cause irritation points which could not be reached while wearing
the “Moonsuit”. Sitting for an hour in the crewroom
I was scheduled
for a high zoom flight to 65.000’,
and after the required pre-breathing
I carried my portable oxygen unit out to my F104C, 56-899, strapped in,
converted to the aircraft oxygen system and departed for the
high speed area “Stovepipe” up over
My scheduled
profile was to climb to 36,000’ a level, run out to Mach 1.7
in full AB and a pull to 1.5 G. When the machmeter showed Mach 2 or
better, I was to then increase to 3G for the zoom. At 38,000’ the machmeter
was indicating Mach 2.1 with about 35 degrees nose up. The airplane was zooming
like an angel and we rapidly passed 50.000’ where all indications were normal.
As the airplane
neared 60.000’ I had to throttle back to keep the EGT within limits. The AB
blew out and when the throttle was near idle I heard slight “thump” down the
back end but all seemed normal. The Starfighter was still climbing but at a
reduced angle of attack, about 20 degrees. As
65,000’ was reached I stop-cocked the throttle to prevent an overspeed
over temp. and eased the stick forward to about level attitude. The cockpit de-pressurised
and I felt the suit pressure come on. It was like being in in an all-over G suit
and it was difficult to move my arms or legs. The outside light was poor due to
the blue/black sky and I had to pull out the instrument panel shades to help the
cockpit lighting.
I thought that
the aircraft would start to descend but, to my amazement, the we kept climbing
in a level flight attitude. As we reached 70.000’,
I eased the stick forward to get a more nose down attitude. The airspeed was
about 155 knots and the attitude changed but the Starfighter kept slowly
climbing until it peaked at 72,300’ when it started to pitch down and descend
with wings level. As the speed increased I popped the speed brakes, slowly
increased the dive angle, and commenced a glorious high speed dive down to lower
levels.
At 40.000’ I
tried a relight without success. At 35,00’ I tried another relight procedure
with same result. At 33,000’ I managed to get a relight
and was delighted to see the RPM and EGT started to rise. With everything
appearing normal I turned towards George passing over the base at 30,000’
prior to entering the pattern. At this stage I knew something was wrong, as an
increased throttle movement produced the desired RPM but no apparent increase in
thrust.
Fortunately, I
was aware of the nozzle failure problem where the nozzles remain open and you
have a perfectly good engine but no thrust. This was my situation then.
The book indicated that level flight could be maintained at 2000’ above
sea level in this configuration. With the altitude at George at 1800’ I was
not about to test this theory. At 25,000’and descending I declared an
emergency and requested a straight-in to
On final
approach the engine was developing a little thrust but I continued the deadstick
approach, dropping the gear at 250 knots and touching down well into the lake
bed at about 185 knots. When I came to a stop,
After the
maintenance crew at the Test Pilot’s School had completed the engine oil/fuel
nozzle control modification 56-899 flew on for some years before being destroyed
in an accident in